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投稿时间:2024-12-09 修订日期:2024-12-09
投稿时间:2024-12-09 修订日期:2024-12-09
中文摘要: 本文以某500kV变电站母差保护误动作事件为研究对象,通过现场检查、复现试验和理论分析,系统地探讨了两点接地引发保护误动作的机制。通过接地网等效模型的分析与试验验证,进一步量化了两点接地感应电流大小及其对保护动作的影响范围。基于研究结论,本文提出了改善二次回路设计、规范作业流程的改进建议,为电网运行维护提供了理论支撑和实践指导。
Abstract:This paper takes the event of a mother differential protection malfunction at a 500kV substation as the research object, and systematically explores the mechanism of protection malfunction caused by two-point grounding through on-site inspection, reproduction experiments, and theoretical analysis. Through the analysis and experimental verification of the equivalent model of the grounding grid, the paper further quantifies the size of the induced current caused by two-point grounding and its influence range on the protection action. Based on the research conclusions, the paper proposes improvement suggestions for the secondary circuit design and standardized operation procedures, providing theoretical support and practical guidance for the operation and maintenance of the power grid.
文章编号:20241209002 中图分类号: 文献标志码:
基金项目:XXXX科技项目(XXXXX)
作者 | 单位 | 邮编 |
代奇迹* | 贵州电网有限责任公司电力科学研究院 | 400044 |
王宇 | 贵州电网有限责任公司电力科学研究院 | |
韩雪 | 贵州电网有限责任公司电力科学研究院 | |
高吉普 | 贵州电网有限责任公司电力科学研究院 | |
张钥朗 | 贵州电网有限责任公司电力科学研究院 | |
李堃 | 贵州电网有限责任公司电力科学研究院 | |
姜骞 | 贵州电网有限责任公司电力科学研究院 |
Author Name | Affiliation | Postcode |
DAI Qiji | 1 | 400044 |
WANG Yu | 1 | |
HAN Xue | 1 | |
GAO Jipu | 1 | |
ZHANG Yuelang | 1 | |
LI Kun | 1 | |
JIANG Qian | 1 |
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